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Daisy Build Report 2 |
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April 29, 2001
Despite some setbacks, building is proceeding at an
acceptable pace.
The biggest setback was our giving up on the homemade
speed controllers; they are malfunctioning and there
isn't time to debug them right now. Shows what you get
using a schematic off of the internet! Still, it's been
educational and I bet we'll get them working eventually.
Just not for SF.
So instead we are going with Innovation First Victor 883
speed controllers, which seem to be working just fine.
As a side effect, the overpowered and complicated
microcontroller setup has been discarded as well for
now, which costs a little flexibility but should pay off
in reliability.
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First step: attach the wheels to the
motors. For wheel hubs, we used some QD bushings
from McMaster Carr, which we were able to bolt
directly to the wheels. After that, all we really
had to do was cut a keyway into the axles and add
some shaft collars to stop the wheels from moving
around.
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The wheels and hubs, on the motors,
with the motor mounts. |
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Once the motors were attached to the
wheels, we attached them to the base. There are
bearings (not ball bearings, just oiled bronze
bushings really) supporting the wheel on either side
so the motor shafts don't take any stress. The
bearings and the motor mount are supported by a 1/4
inch piece of rubber sheet, which allows everything
to move a bit if the axles get slightly bent or
otherwise damaged.
Vacuum cleaner belts are stretched around the wheels
and get pretty good traction. They still need to be
glued and screwed into place but we will surely
destroy one set during drive testing so we'll wait
for the glue anyway.
The little protrusion on the bottom of this picture
was for a contoured front, which has been discarded
now in the interest of saving weight.
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After cutting aluminum sheet into
armor, 3/4 inch aluminum tube into frame parts, and
using about 70 hardened steel machine screws, Daisy
really started taking shape, so we wired it up
messily and took it out for a spin.
It is still only 34 pounds so we can't say
definitively but it seems to be pretty quick and
durable -- smashing into things doesn't seem to hurt
it. Didn't measure the speed exactly but it seems to
be about the expected 10 miles per hour or so.
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We are using an Ohmark mixer in
place of our old PowerPC control processor. It seems
kind of touchy, which I had pretty much expected --
with the old processor we were free to program an
extended dead zone and an exponential response curve
for more precise turning, but it looks like we'll
have to replace that with driving practice. It
wouldn't be too hard to make our own mixer out of a
tiny AVR chip, that could do most of what we want,
but time is getting short.
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So really we could stop and go with
it pretty much like it is, but what fun is a boxy
wedge? The box is really supposed to be a carrier
for the weapon.
We have this nifty standard-issue EV Warrior motor
and a bunch of half-inch shafts, so we got a 5/16 to
1/2 spacer/bushing thing, reamed it out a tiny bit
to fit the metric motor shaft and cut out some slots
so it will slide into the pin sticking out of the
motor shaft (that rolled spring steel pin seems
pretty strong to us so we won't bother replacing it
with something else).
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The motor will attach to the weapon
with a half inch (V4) belt via 3 inch pulleys (1:1
ratio). Hopefully the pulley/belt mechanism will
allow a little slippage and reduce the shock on the
motor when something crunchy gets in the way.
Ideally it will even prevent the motor from stalling
to limit the current a bit, but that might be asking
a bit much.
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Here's what we're talkin'
about! |
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This assembly weighs about nine
pounds. The sharpened stainless steel "petals" sit
in grooves we cut into the barbell weight so they
can't go anywhere and then they are securely bolted
on tight with six military spec steel bolts.
Our only worry is that it will be too heavy for the
EV warrior to spin up energetically. Time will tell!
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